Well, here's the follow up to m overdrive saga:
I tried to disassemble the old solenoid to see if I could reconnect the wire inside. Don't bother - when it breaks, it breaks, and the whole coil is glued inside. Once disassembled, it stays disassembled.
Rob asked if everything was clean. Well, I tried to keep it so, but you know about the best-laid plans of mice... Kickdown cable indeed worked freely and properly.
Brik suggested leaving out the inner o-ring. This was something I had already thought about as a test measure, but I wanted to try the poor man's flush first. There is a pressure test port just below the solenoid, but I don't know whether it tests ahead or behind the solenoid... this morning I got a bucket under this port, took the plug out and hung a rag over the hole to deflect the fluid into the bucket. Bad idea - the rag got tossed off immediately. After mopping up two liters of ATF from the garage floor and putting fresh ATF in, I test drove the car - no improvement, still no overdrive.
Next I unbolted the new solenoid and tested the voltage - electricity was getting to the solenoid, and the transmisssion provided a good ground. I left the ignition switched on and crawled under the car, grabbed the loose solenoid and touched it to the car repeatedly, and got a satisfying click each time. I grabbed a can of brake cleaner and blasted it through the ports in the solenoid in both directions to verify that the ports were opening and closing...being careful with a flammable solvent around a sparking device!
After verifying proper operation, I removed the inner o-ring and bolted the solenoid back on. The results were a bit unexpected -- the overdrive worked perfectly, to the point of switching on and off with the button! I would have expected the missing o-ring to allow fluid to bypass the solenoid, but maybe not. Drove the car about 30 minutes, all was well so I reinstalled the center o-ring. Now everything is as it should be, and the overdrive works. Thanks to the folks who read my message and responded.
My theory: I dunno...maybe there was some junk left over from assembly inside the solenoid, or a chunk of crud fell in the port and got pumped into the solenoid the first time the car was cranked. At this point, I'm too relieved to care much!
|